Analysis of Process Fan Failure & Bearing Housing Case_Study - [PDF Document] (2024)

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    CASE STUDY

    ANALYSIS OF PROCESS FAN FAILURE

    AND BEARING HOUSING/SHAFT DESIGN

    Ken Singleton

    Manager

    KSC Consulting LLC, Bristol VA

    [emailprotected]

    Alan Barbee

    Reliability Engineer

    Fortron Industries

    Wilmington NC

    Bob Bracher

    ATK Maintenance Engineering Assistant

    Radford VA

    Bob McGinnis, P.E.

    (Consulting to KSC)

    McGinnis Engineering LLC, Kingsport TN

    Abstract:AnAir Movement and Control Association (AMCA)Arrangement 8 fan handling hot processgas experienced severalbearing failures and ultimately a catastrophic failure requiringshutdown of the

    plants production. The investigation found that the 1st criticalof the fan rotor was too close to the

    operating speed resulting in excessive bearing loads and shortbearing life. Rotor dynamic modeling was

    used to evaluate a new shaft design. A new shaft and one-piecebearing housing were designed, fabricated

    and installed, successfully moving the critical speed severalhundred RPM above running speed. The new

    design also provided improved maintainability over commerciallyavailable designs, as well as lowering

    vibration and significantly improving reliability. This articlediscusses the analysis process, rotor

    modeling, bearing housing design process, vibration datacomparison before and after the new shaft and

    bearing housing were installed.

    Keywords:Bearing housing design; critical speed; failureanalysis; overhung fan; shaft design; rotordynamic analysis.

    Background: The AMCA Arrangement 8 fan, shown in Figure

    1, was designed for 450F gas temperature. Operating speedwas

    1785 RPM, direct driven by a 200 HP motor using a Falk Grid

    type coupling with 7 spacer. The bearings were spherical

    roller 22218 CCK C3 fit lubricated with Mobilith AW-2grease.

    The fan wheel was constructed of Avesta 2204, continuously

    welded with a 304L SS hub. The wheel hub fit to the shaftwaswith a tapered interference fit, set screws and an end cap.A

    Durametallic Triple Carbon Ring seal provided sealing at the

    shaft entry to the fan housing. The fan base was fabricatedof

    A36 HRS (hot rolled steel). The fan housing was constructedof

    304 SS. Fan performance was 34,200 CFM, SP 22.6, and

    operating inlet temperature of 365F to 392F.

    Figure 1. AMCA Arrangement 8 Fan

    Drawings.

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    Figure 3. Image Taken

    Shortly After Fan Failure.

    Figure 6. Fan Shaft and Fan

    Hub. Shaft Heavy Rub Against

    Fan Wheel.

    Figure 4. Fan Shaft and Wheel in

    Shop After Failure.Figure 5. Mechanical Seal

    Housing.

    Figure 7. All Fan Wheel

    Hubs Failed.

    Fan Reliability: Initial involvement on the project for KSC wasproviding assistance improving reliability

    of the fans. The plant had nine process fans and improving theirreliability was a priority. One

    improvement was replacing the bearing support plates on some ofthe fans with 1-3/4 thick plates

    machined flat to 0.002 inch/ft.

    Bearing reliability and elevated vibration levels continued tobe the primary concerns for this particular fan.

    Analysis of the vibration data identified the need for higherresolution spectra to see the rotor critical.

    The fan rotor 1stcritical is indicated at 1965

    CPM in the data shown in Figure 2. The

    sidebands about 1X and 2X run speed are

    the difference frequency between rotor 1X

    and the rotor 1stcritical. Amplitude

    modulation by the fan rotor 1stcritical

    frequency is apparent in the data. The 1st

    critical frequency would shift higher and

    lower depending on the condition of the

    bearings. New bearings, having tighter

    clearance and higher direct stiffness, would

    shift the critical speed higher. It was found

    that by monitoring the frequency of the 1st

    critical that as the bearings wore the criticalspeed would movecloser to the run speed

    frequency. Vibration levels would begin to

    rapidly increase as the critical speed

    envelope enclosed the running speed

    frequency range. Monitoring the frequency

    of the 1stcritical provided another indicator

    when to replace the bearings.

    Fan Catastrophic Failure: On January 5th, 2006 the fan vibrationlevels were rapidly increasing.

    Vibration data was measured several times that day with the lastdata measured about 5:00PM. That

    evening the fan failed catastrophically. Fortunately no one wasnear the machine at that time.

    One of the first images taken of

    the fan shortly after the failure is

    shown in Figure 3. Bothbearing housings (cast iron)

    fractured. The fan shaft had a

    significant permanent

    deformation (bend) in the area of

    the mechanical seal, see Figure

    4. The shaft at the mechanical

    seal area, see Figure 5, showed

    heavy rub part way around the

    circumference of the shaft.

    Figure 2. Spectrum at Fan Inboard Brg Horizontal

    Shows Fan Rotor 1stCritical at 1965 CPM, 173 CPM

    Above Running Speed. Sidebands About 1X and 2X

    Run Speed are Modulated by the Fan Rotor 1stCritical

    Frequency.

    Fan

    1X

    Fan Rotor

    1stCritical.

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    Heaviest rubbing had occurred near the bottom of the sealhousing. The shaft also exhibited heavy rubbing

    by the fan wheel, see Figure 6,after all of the wheel hub boltsfailed, see Figure 7. The shaft rub locations

    and the bend in the shaft suggested a significant thermal bow inthe shaft may have developed due to

    rubbing at the seal.

    Two vibration spectra and time waveforms measured shortly beforethe failure are shown in Figure 8 & 9.

    The bearing housing vibration does not show a pure sinusoidalresponse but a 1X & 2X response. The

    shaft was likely contacting the seal housing when these datawere taken. The bearing housing hold down

    bolts may also have loosened.

    Near Catastrophic Failure: The fan was returned to service afterreplacing

    the bearings, shaft, fan wheel and mechanical seal. Reliabilityof the bearings

    was a continuing problem. A near catastrophic failure occurredNovember 6,

    2006. The fan was disassembled and physical inspection was madeof the

    rotor and bearings. To include all stake holders in theinvestigation and

    resolution of the fan reliability problems, the clientsreliability engineer had

    assembled a fan reliability improvement team that included thereliability

    engineer (team leader), mechanics, operators, maintenanceplanner and the

    vibration analyst.

    The wheel end bearing was an fa*g 22218 ESK C4 with a steeldouble cage.

    The grease was very dark indicating contamination, as shown inFigure 10.

    The bearing outer race and housing bore exhibited severefretting corrosion.

    The bearing cage at the wheel end exhibited axial wear from therollers

    rubbing. The cage bore exhibited rubbing on the inner race. Theinner race

    had guide grooves machined for the seals.

    The coupling end bearing was also an fa*g 22218

    ESK C4 with a steel double cage. This bearing was

    the fixed bearing taking the thrust load. The thrust

    should have been carried by the higher radially

    loaded wheel end bearing. The grease was very

    dark indicating contamination. The bearing outerrace and housingbore exhibited severe fretting

    corrosion primarily in the top half of the housing.

    Static load on the bearing would have been

    vertically up due to the overhung load of the

    wheel. The bearing cage exhibited axial wear from

    roller rubbing. Rubbing had also occurred in the

    bore of the cage against the bearing inner race.

    The inner race also had guide grooves machined

    for the seals.

    Figure 10. Fan End

    Bearing Nov 6, 2006.

    Figure 8. Fan Coupling End Bearing Housing,

    Horizontal.

    Figure 9. Fan Wheel End Bearing Housing,

    Horizontal.

    Figure 11. Fan Rotor Removed From Service.

    Light Fretting

    Corrosion At

    Bearin Fit

    Greater Wear at Seal

    Area nearest Wheel.

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    The fan shaft exhibited lite fretting corrosion at the heavierloaded wheel end bearing fit, as shown in

    Figure 11. There was also lite wear at the mechanical seal areaand the seal area exhibited melted material

    (product in the air stream). The reported melt temperature was230 Deg C ~ 446 Deg F. There were no

    indications of wheel rub or shaft cracks.

    The bearings were sent to SKF for analysis and their commentswere as follows:

    Classic description of high unbalance load. The cage acts like ahula-hoop orbiting in the bearing about the inner race. The cagebore is very

    difficult to lubricate and thus begins to wear.

    Consider a bearing with a hardened steel cage as an option222218EK.

    The fretting corrosion problem is caused by relative motion ofthe outer race and housing bore. If a

    groove is worn only a few thousands deep in the housing, theouter race can hang and not float

    axially. If this happens the bearing temperature will rise.

    Consider a four bolt housing FSAF 22518.

    Pay attention to color of the grease expelled from the seals.Dark color indicates contamination.

    Vibration data was measured on the fan inboard bearing housingjust prior to the November 5, 2006 event,

    see Figure 12, and Nov 11, 2006 after replacing the bearings,see Figure 13. The data shows the rotor 1st

    critical shifting about 120 CPM higher due to new bearings withno wear having higher direct stiffness.

    During this time period several changes were made includingreplacing the bearing hold down bolts with

    grade 8 bolts and washers, different grease lubrication wastried and bearing clearance was increased

    Fan Rotor-Bearing Dynamic Model: The rotor

    was initially modeled in November 2006 using

    finite element rotor modeling software. The OEM

    shaft was 3.187 inch straight shafting. The 1st

    critical calculated for the original shaft material of

    304SS to just above the fan run speed range as

    shown by the undamped critical speed map inFigure 14. Bearingstiffness was estimated to be

    about 235,000 lbf/in.

    During discussion about machining a replacement

    shaft, there were questions about the shaft material

    to use. The rotor model was run for shaft material

    properties of 304, 316L, 17-4 H 1025 and 4140.

    The wheel weight was determined by measurement

    and the wheel inertial properties were provided by the fan OEM.The coupling weight, bearing locations

    Figure 13. Fan Inboard Bearing Horizontal, High

    Resolution Spectrum, Rotor & BearingsChanged After Nov 5,2006 Outage. Rotor 1

    st

    Critical Shifted to 1980 CPM.

    1stCritical 1980 CPM.1stCritical 1860 CPM.

    Figure 12. Fan Inboard Bearing Horizontal, High

    Resolution Spectrum, Just Before ShutdownNovember 5, 2006.

    Figure 14. Undamped Critical Speed Map for The

    Original 3-3/16 Fan Rotor.

    1st

    2nd

    3rdCritical

    Run Speed

    Estimated Brg

    Stiffness (K) lbf/in

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    and shaft dimensions were obtained from an OEM drawing.Calculations were made to determine the

    following:

    Rotor 1stcritical speed.

    Rotor static deflection.

    Bearing reaction loads.

    Rotor response to unbalance at the fan wheel center ofgravity.Undamped critical speed map of rotor versus bearingstiffness.

    Maximum static shaft stress in bending.

    Effect on rotor critical speed with 17-4 shaft diameterincreased from 3.187 to 3.25 inch.

    Effect on rotor critical speed with 17-4 shaft diameterincreased from 3.187 to 4.00 inch.

    Residual static and couple unbalance tolerances for BalanceQuality Grade G2.5 calculated per ISO

    1940-1.

    As expected, the different modulus of elasticity for each shaftmaterial had little effect on the calculated

    shaft 1stcritical speed. Material 4140 had the highest modulusof elasticity and calculated to have a critical

    speed about 50 RPM higher than the stainless steelmaterials.

    Shaft diameter changes were evaluated for increasing the1stcritical speed. Shifting the wheel end bearing

    closer to the fan wheel was also considered. Increasing theshaft diameter from 3.187 to 4.00 inch at alllocations except thecoupling hub and the tapered wheel hub fit and using 17-4 SS waspredicted to raise

    the 1stcritical speed 30%. This appeared to be an effectiveoption to shift the critical speed and increase

    shaft stiffness but would require lowering the bearing supportplate to accommodate larger bearings and

    housings.

    New Rotor and Bearing Housing Design Development: Afterevaluating the options to increase the

    shaft size to move the 1stcritical speed higher and the bearingand support plate changes, a decision was

    made to use a one piece bearing housing. Quotes were requestedfrom a well known bearing supplier for a

    tunnel type bearing and shaft assembly. Delivery was severalmonths since these bearing housings are not

    a stock item and are manufactured in Europe. Additionally, theshaft options offered by the bearing

    supplier did not provide the larger diameter at the fan end thatwas needed to shift the critical speed higher.

    In addition, the tunnel bearing housing centerline height wasdifferent than the SAF Pillow Block housings

    which would require lowering the bearing support plate.

    The clients reliability engineerand the fan reliabilityimprovement team evaluated all these options. After

    following a very methodical process, a decision was made for KSCto design the bearing housing and shaft

    assembly and to use a local machine shop for fabrication of theshaft and bearing housing assembly. The

    client would review and approve the design and drawings.

    The team wanted the bearing housing to be

    designed for direct swap out of the existing pillow

    block bearings, something the off the shelf bearing

    housing design would not accommodate. This

    meant that the shaft centerline height and bolt

    pattern would match the existing SAF 218 bearing

    housings and the fans position axially within the

    fan housing had to be maintained. The design

    would provide a backup plan if the new bearing

    housing and shaft design did not work and it was

    necessary to reinstall the original shaft and bearing

    housings. The team wanted all of the components

    to be assembled from one end, so that the fan

    wheel did not have to be removed from the shaft Figure 15. Modelof Final Shaft Design.

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    during bearing replacement. Removing the fan wheel from theshaft was a major, time consuming job.

    These details were incorporated into the bearing housing andshaft design as well as other features to

    optimize lubrication, vibration analysis, and temperaturemonitoring.

    Over several weeks the design was developed and refined perinput from the clientsreliability team. The

    rotor final design model with the 1stcritical mode shape isshown in Figure 15. The 1stcritical was

    predicted at about 2475 RPM providing about 27.7% separationfrom run speed. Rotor weight and bearing

    reaction loading calculated as follows:

    Shaft wt: 115.35 lbf

    Total Rotor wt: 694.35 lbf

    Coupling end bearing reaction: -333 lbf

    Fan end bearing reaction: 1,027 lbf

    The damped unbalanced response for the wheel end bearing isshown in Figure 16and the 3D plot of the

    rotor displacement in mils pk-pk at run speed is shown in Figure17.

    Rotor Bending Stresses: The team leader asked for the maximumbending stresses in the fan rotor and the

    location of those stresses. The stresses were calculated usingDyRoBeS [3,4] rotor modeling software for the

    static bending stresses in the original rotor, see Figure 18,and the redesigned rotor Figure 19. However,

    additional calculations must be made to evaluate if thesestresses are acceptable.

    Figure 16. Undamped Critical Speed Map for

    The Original 3-3/16 Fan Rotor.

    Figure 17. Shaft Damped Unbalanced Response

    to G2.5 Balance Quality Grade at Run Speed.

    Figure 18. Static Bending Stresses, OEM Shaft

    304SS, Maximum 2417 psi at Wheel End Bearing.

    Figure 19. Static Bending Stresses, New Shaft

    Design, 316l SS, Maximum 2016 psi Inboard

    Wheel End Brg.

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    According to [2], to allow for lack of complete designinformation, design texts, handbooks, and engineering

    codes recommend use of safety factors and service factors. Thedesign of machine members is dominated

    by the concept of allowable working stress. This stress levelwhich should not be exceeded is a fraction of

    either the ultimate, yield or fatigue strength of the material.For static loading, yield or ultimate strength is

    needed. Cyclic loading is called material fatigue. Thetransition in strength from static to cyclic loading

    strength drops to 90% of the initial static value after about1000 cycles and to about 50% after 1 million

    cycles then the curve is fairly flat thereafter. The deratingfactors [2]used to determine the allowable

    working stress in bending for the redesigned shaft using 316 SSare as follows:

    Se= Endurance limit/fatigue limit of machine component

    S'e=Endurance limit/fatigue limit of a rotating beam specimen ofthe same material.

    ka= Surface finish derating factor. Polished surfaces have lowerderating factor than rough

    machine surface.

    kb= Size finish derating factor.

    kc= Reliability derating factor.

    kd= Temperature derating factor.

    ke = Stress concentration derating factor.

    kf= Impact derating factor.

    The calculated allowable working stress of 7,126 psi was greaterthan the values allowed by MIL STD 167[6]. The factor of safety isthe allowable working stress divided by the stresses in bendingwhich calculated

    to 3.5. A factor of 2 it typically recommended.

    Bearing Housing Design Process: The bearing housing and shaftassembly, shown in Figure 20, were the

    end result of the design process. The bearing housing body wasfabricated from mechanical tubing. The

    mounting feet were fabricated of mild steel and welded to themain body. The bottoms of the feet were

    machined flat to within 0.001 and coplanar to within 0.0015.Dowelholes were provided in the feet foraccurate location of thebearing housing when mounted to the fan pedestal. The bearing boreswere held to

    guidelines published by SKF for size, concentricity, run-out andperpendicularity. Two grease purge holes

    were drilled and tapped -14 NPT, centered between bearings andpositioned 45 off axis below center.

    Three -28 tapped holes with spot facing were provided (1) topvertically and (2) horizontally each side

    for the mounting of accelerometers directly over each bearing.One -18 NPT tapped hole was provided

    at each bearing for a temperature probe.

    k S' 55,000 35,000k = 0.35S' 0.5 0.5 200,000a e

    a

    e utS

    ' 35,000psi FromChart Pg3.22 Ref 2a ek S

    35,000' 58,333

    0.6e

    S

    k =0.75 Where d>2.0inb

    k =0.702Where Reliability = 99.99%c

    620 620k = = 1.1

    460 460 100d

    T

    1 1k = 0.54

    1.86e

    fk

    S = 'e a b c d e f ek k k k k k S S =0.35 0.75 0.702 1.1 0.541.86 35,0000=7,126psie

    Where NotchSensitivity

    g = 60 From Chart 3-15,Pg60 Ref 2

    1 ( 1) 1 0.86(1 1) 1.86

    f

    f t

    k

    k g k

    7,126Factor of Safety = 3.5

    2,016

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    Figure 22. Detail of Coupling End of Bearing

    Housing Showing Seal and Seal Path.

    A labyrinth ring was attached to the fan end of the

    bearing housing by bolts, as shown in Figure 21.

    The labyrinth provided a non-contact seal. The

    design maintained 0.010 radial clearance between

    the minor diameter of the ring and the outside

    diameter of the shaft. The labyrinth ring bore was

    profiled to form three recessed grooves. These

    recessed grooves provided a non-contacting grease

    seal between the outside contaminates and the

    bearing.

    The seal ring was made from 6061 aluminum to

    prevent damage to the shaft if a rub occurred

    against the shaft. A V-Ring Dirt Excluder was

    added as a supplemental seal to repel dust. The V-

    Ring fit snuggly over the shaft and sealed against

    the outer face of the static labyrinth ring.

    Two grooves were machined in the inner diameter

    of the end cap to serve as a type of labyrinth seal, as shown inFigure 22. A

    V-Ring Dirt Excluder (14) was also provided as a supplementalseal. Thegrooves in the end cap were sized so that the bore couldbe machined if

    required, removing the grooves, to receive a 90 x 110 lip seal.This provided

    for use of a lip seal if the labyrinth seal and grease provedinadequate. A seal

    path or sleeve was installed with a shrink fit to the O.D. ofthe shaft to

    provide a wear surface for the lip seal. A seal path provides ameans of

    renewing the shaft seal contacting surface without having toreclaim the shaft

    to remove grooving. Adequate hardening along with plungegrinding the

    surface of the seal path offers a superior surface, extendingthe life of the

    seal.

    End Caps: The end caps were tapped for 1/8-27 npt for greaselines, see

    Figure 23. Also provided were -28 holes on the face of the endcap for

    the mounting of accelerometers to measure axial vibration.

    Grease Dams: Grease dams were added inboard of each bearing toretain or

    hold grease close to the rolling elements due to the

    open space in the housing between each bearing,

    Figures 24 & 25.

    Sleeve: In order to facilitate removable of theshaft assemblyfrom one end as requested by the

    fan reliability team, a spacer sleeve was used

    between the bearings, as shown in Figure 26. A

    close fit between the I.D. of the sleeve and the

    O.D. of the shaft was used to minimize residual

    unbalance affects.

    The stack-up tolerance between bearings was

    maintained by an SKF lock nut, KMFE style with

    locking screw.

    Figure 21. Seal at Fan

    End of Brg Housing.

    Figure 20. 3D Model of Bearing Housing and

    Shaft.

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    Drawings of the bearing housing and shaft assembly are shown inFigures 27.

    Fan Wheel/Hub Mounting: The fan wheel hub

    and shaft used a tapered fit. The amount ofadvance controlledthe amount of interference fit

    and the compressive forces of the hub to shaft. Calculationswere made for the following:

    Hub material 304 SS per the fan OEM drawings.

    Two shaft materials were considered, 316 SS and 17-4 PHCondition 1025

    The fan hub and shaft used a tapered fit of 0.750 in/ft per thefan OEM drawings, Figure 28. The shaft,

    hub and wheel material properties are listed in Table I.

    Figure 25.

    Grease Dam at

    Fan End of Brg

    Housing.

    Figure 24. Grease

    Dam at Fan end of

    Brg Housing.

    Figure 26. Bearing Spacer Sleeve.

    Figure 27. Bearing Housing, Shaft, Fan andBearing Support PlateDrawing.

    Figure 28. Shaft Taper Fit Dimensions

    Taper .750 in/ft

    3.187

    Figure 23. End Cap Grease Purge Holes.

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    Modulus @

    400 Deg F

    2% Yield

    Strength psi,

    min

    Coefficient

    Thermal Expansion

    Shaft Material 17-4 1025 27.0E6 psi 145,000 6.1E-6 /Deg F

    Hub Material 304 SS 27.9E6 psi 30,000 9.0E-6 /Deg F

    Shaft Material 316 SS 28.1E6 psi 30,000 9.0E-6 /Deg F

    Wheel Material RA2205 26.6E6 psi 65,000 7.81E-6 /Deg F

    The team asked about the advantages and disadvantages of astraight fit versus a tapered fit. A comparison

    was provided as shown in Table II.

    Advantages of a taper fit: The contact area between bore andshaft can be checked

    The interference between hub and shaft is controllable bythe

    amount of advance of the hub on its shaft

    The removal of hubs is easier

    Disadvantage of a taper fit:

    It is more difficult to accurately machine the tapers of the hubbore

    and the shaft.

    It is possible to overstress the hub if it is advanced too faron the

    shaft taper.

    Dirt and surface imperfections restrain hub advance, and cangivethe false impression that the desired interference wasreached.

    Advantages of Straight fit: A straight fit is more easilymachined and measured.

    Disadvantages of a straight

    fit:

    Assembly without galling is difficult.

    Disassembly without galling is even more difficult.

    Maintaining zero clearance between shaft and hub isdifficult.

    Locking the hub to the shaft requires a step in the shaft andcreates a

    stress riser.

    The specific fan hub advance required to provide

    adequate interference fit at operating speed and

    temperature calculated to 0.0306 inch, Figure 29.

    Equations: Equations are from [1]

    Table I: Material Properties Used For Calculations

    12 d

    A it

    Where:

    A= Hub advance on the taper

    t= Taper (inches/foot)

    d= Shaft nominal diameter (inch)

    i = Interference rate (inches/inch)

    Table II: Advantages/Disadvantages Straight & TaperedFits.[1]

    Figure 29. Illustration of Split Collar

    Installed To Act As Stop When

    Installing Heated Hub.[1]

    0.0306 inch for 316SS Shaft and 304

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    Interference rate is the difference between bore and shaftdiameter (diametrical clearance), divided by the

    shaft diameter. The interference rate is a ratio of quantitieswith the same units and thus has no unit of

    measurement.

    The combined hoop and compressive stress in hubs caused byinterference is maximum at the bore:

    After completing the fan hub and shaft fit calculations, thefindings were as follows:

    1.

    Changing the shaft material to 17-4 PH Condition 1025 offeredsignificant advantages in material

    properties over 304 SS. But, the differential coefficient ofexpansion between the hub and shaft would

    not permit achieving an interference fit at the specifiedrunning speed and operating temperature

    without exceeding the yield strength of the hub. The maximuminterference rate at ambient

    temperature to avoid exceeding the yield strength calculated to0.0006 inch/inch. But, this would

    result in a loose fit of .0016 inch at operating speed andtemperature. In addition to the inability to

    maintain low residual unbalance, the loose fit would causefretting corrosion of the fit.

    2. For shaft material 316 SS and hub material 304 SS a maximuminterference rate of 0.0006 inch/inch at

    ambient temperature calculated to not exceed the specifiedstress limits. At operating speed and

    temperature an interference of 0.001 inch was calculated to bemaintained. For the existing wheel and

    hub, 316 L SS shaft material appeared to be the optimumchoice.

    3.

    Even with a larger shaft diameter of 4.000 inch and lessflexure, there was still some concern about

    uneven rubbing of the seal material against the shaft causingthermal bowing. Thermal bowing would

    cause increased unbalance forces and vibration. Coating the sealcontact area with a ceramic material

    would reduce the coefficient of friction significantly andreduce potential thermal bowing and shaft

    wear. Ceramic coating the seal area was recommended.

    Where:

    i= Interference rate (inch/inch)

    D= Hub bore (large end)

    d= Shaft diameter (large end)

    2 2 2 2

    2 2 2

    ( ) ( )

    2 ( )

    i E d c D d P

    d D c

    Where:

    P= Contact pressure

    i= Interference rate (inch/inch)

    E= Modulus Elasticity Tension

    d= Shaft diameter (large end)D= Hub OD

    c= Shaft hole diameter (if any)

    D di

    d

    4

    2

    3

    1 ( )psi

    P k

    d

    D

    Where:

    = Combined hoop and compressive

    stress in hub psi

    P= Contact pressure psi

    k= d (shaft diameter)/D (hub bore)

    d= shaft diameter

    D= hub bore

    D = Hub bore

    d = Shaft diameter (large end)

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    4. For assembly of the 304 SS hub and 316 SS shaft, use of asplit collar clamped to the shaft was

    recommended to provide controlled 0.0306 inch advance of thehub, as shown in Figure 30. For

    ambient air temperature of 70 Deg F, the hub required heating toabout 200 Deg F prior to installation.

    The hub would be installed on the tapered fit against the splitcollar and the draw bolt hand tightened

    to hold the hub in place while it cooled.

    5.

    Aminimum 70% contact is recommended per

    AGMA Standard 9002-A86 for keyed shafts

    with tapered fits. If the fit does not meet the

    70% minimum, and the fit requires lapping,

    the shaft and hub should not be lapped

    together. A ring and plug type lap of soft

    material such as brass should be used.

    A question was raised by the fan reliability team

    about welding the fan wheel to the hub instead of

    using the bolts originally provided by the fan

    OEM. This question was asked since all of the

    bolts failed during the Nov 6, 2006 failure. See

    Figure 30. A recommendation was made to

    increase the hub-to-fan wheel bolts by 50% in

    diameter. High strength, corrosion resistant bolts,

    should be used and the welding process eliminated. Because ofthe difference in the thermal coefficient of

    expansion between 304 SS and RA 2205, welding could cause weldcracking problems over time if the hub

    and wheel are welded together.

    Bearing Evaluation:Many AGMA Arrangement 8 fans are providedwith spherical roller bearings. Wehave found that the bearings areoften not properly selected for the speed, load and lubrication.This is

    especially true for the coupling end bearing which often doesnot have the minimum loading specified by

    the bearing manufacture. For this fan the spherical rollerbearing limiting speed and required minimum

    loading (using 2% of the dynamic load rating for roller bearingsand 1 % for ball bearings as recommended

    by SKF) calculated as shown in Table II.

    .Bearing Location Fan OEM Design One Piece BearingHousingDesign

    Bearing

    Location

    Fan OEM

    Design

    One Piece

    Bearing

    Housing

    Design

    Coupling End 22218 EK 6217 Deep Groove

    Ball

    Fan End 22218 EK 6320 Deep

    Groove Ball

    Limiting Speed 5300 RPM 5600 RPM Limiting

    Speed

    5300 RPM 4300 RPM

    Static Radial

    Load lbf

    333 lbf 335.5 lbf Static Radial

    Load lbf

    1007 lbf 1031 lbf

    Bearing Static Load

    Rating CO

    84,300 lbf 14,400 lbf Bearing

    Static Load

    Rating CO

    84,300 lbf 31,500 lbf

    Bearing MinimumRequired Load lbf

    1461 lbf 196 lbf BearingMinimum

    RequiredLoad lbf

    1461 lbf 391 lbf

    Did not meet

    Minimum load

    for Grease

    Meets Minimum

    Load

    Did not meet

    Minimum load

    for Grease

    Meets

    Minimum

    Load

    Problems Encountered During The Project: All projects havehiccups as did this one. Obtaining

    accurate information from the fan OEM, the rotor assembly, androtor balancing presented some

    difficulties. During initial rotor balancing, there was damageto the shaft bearing fits. The images of the

    Figure 30. Nov 6, 2006 Failure, All Fan Hub BoltsFailed.

    Table II: Comparison of OEM Specified Spherical Roller Bearingand Ball Bearings Used inCustom Design.

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    Figure 31. Journal Showing Balance Machine

    Roller Damage to Bearing Fit (Coupling End).

    Metal Shaving Embedded in Journal.

    Figure 32. Journal Showing Balance Machine

    Roller Damage to Bearing Fit, Wheel End. This

    Roller Track Appeared Wider or the Shaft

    Shifted Axially During Balancing Operation

    Generating Two Tracks.

    shaft bearing fits, Figures 31, 32show scoring damage to thejournals by the balancing machine rollers.

    Scoring of the shaft journals is always a concern when usingrollers in a balance machine to support the

    shaft. To minimize scoring some actions that can be taken are asfollows:

    The balance machine pedestals and rollers should be alignedperpendicular to the shaft centerline.

    Misalignment of the rollers to the shaft can reduce theroller/shaft contact area and increases the

    stress level. Misalignment can also cause the rollers togenerate an axial thrust increasing scoring

    damage.

    Lubricating oil should be applied to the shaft and rollers atregular intervals to maintain an oil film.

    Felt wipers in good condition should be installed. The feltshould contact the rollers to clean the

    rollers and minimize metal particles being carried between therollers and the shaft.

    The shop performing the rotor assembly and balancing

    did not follow ISO 1940-1 process to determine the correctbalance tolerance. The balance machine

    printout showed that the residual unbalance tolerance used wasfor a center hung rotor which was then

    divided by 2 to obtain the tolerance at each bearing journal.The residual unbalance tolerance should have

    been calculated per ISO 1940-1 to G2.5 for an overhungconfiguration, as shown in Figure 33. The

    calculations are as follows:

    b = 9.625

    c = 30.682

    d = 14.187

    Note that the static residual unbalance for the overhung wheelis about 1/10 of

    the tolerance for the wheel if is center hung. Comparing thecalculatedresidual unbalance tolerances to the shops balance reportshowed the

    following:

    Balanced to 25.893 oz-in Right Side

    Balanced to 20.027 oz-in Left Side.

    These values were far in excess of the calculated maximumresidual

    unbalance values:

    Static unbalance = 0.65 oz-in

    Maximum couple residual unbalance = 2.1 oz-in.

    Two balance facilities were used but the quality of work did notmeet expectations at either facility.

    2 2

    per

    static

    U dU

    C

    Permissibleresidualstaticunbalance

    Permissibleresidual unbalance

    Permissibleresidualcoupleunbalance

    static

    per

    couple

    U

    U

    U

    3

    2 4

    per

    couple

    U dU

    d

    6716.015 2.5 5.61

    1800perU oz in

    5.61 9.6250.65

    2 2 30.682staticU oz in

    5.61 3 9.6252.1

    2 4 14.187coupleU oz in

    b

    d

    c

    Figure 33. Schematic of

    Fan Rotor For Balance

    Calculations.

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    Installation of New Bearing Housing and Shaft: The speciallydesigned bearing housing and rotor were

    installed in Sept 2007. Images of the beefed up bearing supportplate, access panel in the fan housing

    (added to permit in-place balancing and inspection of thewheel), and the bearing housing and shaft are

    shown in Figures 34-37.

    The rotor 1stcritical speed,

    measured in the vibration data.

    was very close to the frequency

    predicted by the rotor model.

    The spectra plots with log

    magnitude scaling, see Figure

    38, were measured on the fan

    outboard bearing housing

    horizontal direction and showsthe rotor 1stcritical speed of

    2351 CPM shortly after startup.

    Figure 34. Photos of Newly Installed One

    Piece Bearing Housing.

    Figure 35. Photo of Newly Installed One

    Piece Bearing Housing With

    Accelerometers and Temperature

    Sensors Installed.

    Figure 36. Close Up Photo of Newly InstalledOne Piece BearingHousing With

    Accelerometers and Temperature Sensors

    Installed.

    Figure 37. Photo of Modified FanHousing to Install Access Panelfor In-

    Place Balancing & Inspection.

    Figure 38. Frequency Spectra at Fan OB

    Brg Housing, Hor, Original Shaft &

    Bearings Top Plot, New Design Brg

    Housing and Rotor Lower Plot.

    1X

    1X

    Rotor 1stCritical (as low as1860 CPM) With OriginalShaft &SAF 518 Housing &

    22218 Spherical Roller

    Rotor 1stCritical 2351 CPM

    with Custom Design OnePiece Bearing Housing, Shaft& BallBearin s.

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    Before & After Vibration: The overall and 1X vibrationin/sec pk are shown in Figures 39 & 40.

    Conclusions:

    1.

    The specially designed one piece bearing housing, shaft andbearing assembly successfully raised

    the fan rotor 1stcritical from 1860 RPM to about 2350 RPMproviding a separation margin of

    around 24% from run speed. The design provided severaladvantages over an off-the-shelf one

    piece bearing housing and shaft assembly. The major advantageswere (1) direct bolt in-place

    with hold down bolt holes matching the base plate existingholes; (2) lower bending stresses

    generated by the overhung load, (3) improved maintainability(designed to permit bearing

    replacement without pulling the complete rotor or fan wheelremoval), and (4) ball bearings met

    the minimum load guidelines specified by the bearing manufacturefor grease lubrication.

    2. Bearing housing vibration levels were reduced afterinstallation of the one piece bearing housing

    and shaft and continued to remain low until the plant ceasedoperation in 2008.

    3.

    Problems were encountered during the project. Some of theseproblems had to do with the quality

    of work performed at the shops which included excessive runoutof the tapered shaft fit on the 1 st

    shaft, unacceptable balance quality at two balancing facilities,and inaccuracy of some field

    measurements.

    4. Important steps that should be considered for similarprojects:

    a. Detailed analysis of the fan should include but not limitedto vibration, bearing calculations,

    bearing lubrication requirements, bearing housing mounting,bearing support flatness and

    rigidity, foundation, accurate rotor/bearing model, fanperformance curves, review of

    maintenance history and OEM critical speed calculations.

    b. Develop an accurate layout drawing of the fan base, bearingsupport plate, hold down bolt

    locations and bolt size, the fan housing, wheel dimensions,wheel axial position, the inlet cone

    position and overlap.c. During fabrication and machining,witness dimensional inspections of the bearing housing

    and shaft at the machine shop. Shaft runout measurements shouldbe done with the rotor

    supported in V-blocks at the journals per API 687. Dont trust acoordinate machine

    measurement machine to accurately measure shaft runout andfits.

    d. If using a contract balance shop, conduct detailed inspectionof the balancing facility to

    determine training level of personnel, condition of thebalancing machine, most recent

    calibration date and capability to perform the requestedbalancing work.

    Figure 39. Chart Fan Bearing Overall Vibration

    Original Design and Modified Design.Figure 40. Chart Fan 1XVibration in/sec pk

    Modified Bearing Housings & Shaft.

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    References:

    1. Michael M. Calistrat,Flexible Couplings Their DesignSelection And Use, ISBN 0-9643099-3.

    2. Hindhede, Uffe, Zimmerman, John R., Hopkins, R. Bruce,Erisman, Ralph J., Hull, Wendell C.,

    Lang, John e., Machine Design Fundamentals, A PracticalApproach, ISBN 0-471-04136-X.

    3. Chen, W.J., Ph.D., P.E., Gunter, C.J.,Ph.D.,www.DyRoBeS.com

    4. Chen, W.J., Ph.D., P.E., Gunter, C.J., Ph.D., Introduction toDynamics of Rotor-Bearing

    Systems, ISBN: 978-1-4120-5190-3.5.

    Gunter, Edgar J., Understating Amplitude And Phase in RotatingMachinery, RODYN Vibration

    Analysis, Inc., Charlottesville, Virginia, Vibration Institute33 Annual Meeting June 24-26, 2009.

    6.

    Szenasi, Fred R., P.E., Torsional Analysis of Variable FrequencyDrives, Engineering Dynamics,

    Inc. San Antonio, Texas

    http://www.dyrobes.com/http://www.dyrobes.com/http://www.dyrobes.com/http://www.dyrobes.com/
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